Bailey Steam
Engineering Designs


6" Mc Laren Build Diary

Part two of the 6" Scale Mc Laren Road Loco build

Introduction

The Build diary had started to get too large. Personally, I do not like web pages that take so long to load that you loose interest before you get to see the content. This prompted the decision to split the diary following the August update. To start this new section I will add several recent photo's of the engine. Part two of this diary will include some details of assembly, valve timing, running on compressed air and putting the engine to steam for the first time.

 

The con rods are now complete so is most of the other small parts. Erecting and final assembly of the valve gear & motion has now taken place. Including the fitting of the flywheel. Adding the flywheel to the crank has made it one of the few assemblies that had to be moved with the lifting hoist.

It is surprising how long assembly takes. All of the small jobs, threaded holes, small details or finishes that have to be added to a part to complete it. It is always tempting to rush ahead and get the engine running on air or steam without completely finishing the mechanical parts. I try and make everything first then assemble it to the main part of the engine.

View of the HP slide valve, cylinder now fixed to the boiler! : Note the size of the LP steam passage!

The flywheel was a very nice fit on to the crankshaft. I did not want to distress the crank while fitting the flywheel so I decided to heat the flywheel up to allow it to slide into position. The machined key seat for the flywheel had to be lined up during assembly to allow the key to be fitted later. To align the key slots I made up a small cube of steel this was adjusted so that it would slide the complete length of the key slot in both the flywheel and the crankshaft.

The flywheel was warmed using a fairly large propane torch, the flame was moved round and over the surface to allow gentle expansion of the whole area without distortion. When hot. the flywheel was laid down onto two wooden blocks that supported the flywheel off the ground and to the correct and final resting place. The small alignment cube was inserted into the flywheel key seat followed by the crank. The crank inserted easily due to the heat in the flywheel.

Gaskets were made from 1/32" graphite paper for the steam chest and cylinder covers. The cylinder had to be positioned and lined up correctly with the con rods and with the centre line of the boiler (crank). To do this is a lot of messing around. I fitted the pistons to the crossheads, con rods etc to the engine. Rotating the flywheel allowed the cylinder - Stroke position to be found. I have allowed a total of 1/32" mechanical clearance & 1/32" for the gasket paper for the front cylinder cover when the engine is cold.

When the engine is steamed the boiler expands with heat and pushes the cylinder forward about 0.080". This has to be allowed for during the design of the piston length to allow clearance of the rear cover when hot. The cylinder was aligned with the boiler (& crank) centre line using an engineers spirit level. The type used for machine tool installation. The boiler was drilled and threaded 1/2" BSF (nice thread) to secure the cylinder. So how do you seal the boiler and cylinder? I have tried using high temperature silicone sealant from Screwfix. This product has a working temperature of up to 300 degrees centigrade. Hope it works!

View of the valve gear swung back out of the way

Valve timing on a large engine can be a trial. I find it easier to find top dead centre (TDC) for the crankshaft then remove the connecting rods to allow the engine to turn easier, especially if the piston rings have been fitted. To find TDC I use a dial test indicator (DTI). Place the DTI close to the limit of crosshead travel. fine adjust the DTI and crank position so that you can measure the last five thousands of an inch travel. Make and attach securely a position indicator at the outer edge of the flywheel. At each position either side of TDC mark a small line on the flywheel outer edge. TDC is midpoint of the two marked positions. I usually cut a small notch on the inner edge of the flywheel with a junior hacksaw at TDC. This secures a permanent record for future use if required!

Set square clamped to the horn plate, align the top edge for TDC positions

Valve timing is then easier, I use a small spacer bush on the eccentric bolts to allow me to remove and fit the rear half of the eccentric quickly. During the timing operation the eccentrics are only secure by a enough thread to fill half a nut. With the TDC mark aligned move the eccentric and observe the position for the slide valve. Adjust the valve to be open by 0.010" at TDC is recommenced for the Big Mac when the reversing lever is in the running position, Rotate the flywheel, observe the valve opening position at the other end, if incorrect try centring the slide valve. Several iterations of this in both forward and reverse are required to get the timing pretty good. Good design practice should allow both forward and reverse valve settings to be the same but! If needed, optimise for best timing in the forward direction, this is what you will be using most of the time. Both the HP & LP valves need to be accurately set

Home made disposable ring clamp!

The piston rings were fitted to the pistons, home made ring clamps were made from a small thin (0.012") strip of stainless steel and jubilee clips. This works quite well. The jubilee clips can be unscrewed completely to remove them from the piston rod.

The crosshead trunk guide's are bolted to the wayshaft bracket from below, two fasteners in each guide. Getting the distance between the trunk guide and wayshaft correct requires the addition of packing and shims. I made the packing from 3mm mild steel plate. This was ground to the correct thickness using a surface grinder. This allows a very rigid connection to support the trunk guide from flexing when pulling hard.

The 5-7/8" LP pistons fit easily!

Following the completion of the valve timing all of the boiler washout holes were plugged to seal the boiler for testing on compressed air. I have two small compressors. Both of these were connected to the engine for the air test. The engine ran well on compressed Air. Moving the reversing lever back to mid position made the engine notch up as expected. It is so nice to see the engine run after such a lot of hard work!


Update, April 10th 2004 : To Steam or not to Steam, that is the question?

Having got to this stage it is quite a task to make the right decision, will I run the engine in primer for a steam test, a whole season? What would a steam test do? where will it get me? Lots of questions, possibility's. I reckoned the following, if I steam test the engine I would probably only run it once or twice to make sure it runs well, it should run better on steam than it did on air. Steaming the engine would get the engine coated in oil and soot, this would get baked on to the engine, painting would be a lot harder due to the extra cleaning. I talked this through with steaming friends and concluded it will be better to paint the engine. The engine will be finished when steamed for the first time.

Belly tank internal coated with black bitumen paint

I painted the inside of the belly tank with black bitumen paint to seal it form leaking. This is quite a messy task. The lack of ventilation in the tank causes a very slow drying time. The inside of the tender water tank was also painted. I made a list of items that needed to be done before steaming or painting. It is surprising how much time the little jobs take, some of the little jobs were in fact quite big. I needed to get the wheels riveted. Allen offered to rivet them using the traditional hot riveting method. To speed things up I decided to get them spun riveted. this was done at LSM engineering. LSM have a machine that is capable of spinning 8 mm rivets.

Lashed up grinding method

One remaining job was to grind the vulcanised rubber on the rear tyres. I had previously ground the front tyres a couple of years ago. I lashed up my old valve facing grinder as used for the front wheels. A small geared motor was used to rotate the rear wheel. The gearbox had a pulley and a very long drive belt from a combine harvester. Good having Farming friends. I started the grind, very slow and tedious indeed. In fact I had such a large amount of rubber to remove it was going to take ages. If you try and apply too large a cut the rubber gets hot, then melts in to a sticky mess. It is hard to get out of this situation when this happens!

Turning the wheel rubber with the Webster & Bennett boring machine

Allen & Tom Prout called over, Allen suggested we turn the excess rubber off and groove the tyres using his large Webster & Bennett boring machine. The wheels were loaded in to Allen's van and taken to his engineering works. The wheel looks small on the boring machine even the O/D is 44 inches!

Hacksaw blade tool holder

That evening I made up a special tool holder that would hold a 1/2" hacksaw blade that was heated, bent, ground to profile and tempered. The excess rubber was simply removed using this method. The two grooves were also added using this tool. Cutting the grooves was like parting off a 44 inch rubber blank. the groove could be cut in minutes. The tool was mounted on a small compound slide. The slide was attached to a plate that mounted it in the Webster. I can supply details of how this cutter works on request if anyone would like it.

Rear Wheel before after grooving & Grinding

The edges of the rubber tyres were square after grinding. Radii were ground on the rubber to reproduce the effect of original tyres.

Boiler lagging steel with wood visible on rear section

The boiler is lagged with 12 mm x 12 mm wood. I had to cut the wood to size using a band saw to get the correct thickness. The strips of wood were cut to length and attached to the boiler with Silicone sealer. This works quite well. The boiler lagging steel was rolled from 1 mm mild steel sheet. Lots of accuracy is required to fit the lagging steel. One wrong cut and all is wasted!

2 off M3 pan heads at centre joint of lagging sheets

The lagging sheets were attached to the boiler at the top with 3 mm pan head screws. These fasteners will be filled to replicate the effect of rivets. The 3 mm fastener were threaded in to small pieces of 1/2" x 1/2" mild steel that had been previously welded to the top of the boiler. This would allow me to fix the sheets to the boiler and attach the boiler bands easily.

Boiler band and angle bracket

The boiler bands were guillotine cut from 1/16" brass sheet. The edges of the bands were draw filed to remove the sheared edges. This would be beneficial if I used the band edge as a guide for lining! The boiler bands needed angled brackets that would allow me to fit a fastener that would pull the two ends together. I fabricated these from 1/8" brass. The brass sections were silver soldered together. Quite a lot of filling and fettling was needed to make the brackets nice.

Paint & Colour scheme? Well this could be one of the hardest part's of the build so far. I had trouble finding anyone who could tell me what green to use. This type of engine was produced for the War Ministry and would have been originally painted in plain un-lined drab olive green. I think this would not look too nice. Boadicia is nicely painted I am told the the paint was mixed and is not to a repeatable colour code. So there are the standard Mc Laren colours. Red Wheels , black boiler, tender tanks etc? One of our friends has a young son called Joseph Lowen-Grey or J-Lo as I call him, Jo is a BIG fan of steam and said he would like a green engine, Jo got his wish!

I took some colour photo's to a paint shop in Gloucester to try and get the correct colour. I bought 2.5 litres of RAL6002, looked alright in the shop? I had convinced myself that it would darken with use! Later that day, Allen and Tom Prout called over with Richard Hunter to view the progress. Ransoms green was the conclusion! I had chosen a nice shade of Ransoms green. This would look stupid on the engine. I returned the pain to Gloucester to get the colour adjusted. Blue and black was added in large quantity's to reduce the colour. I thought it would be fine after the change. Allen called over later in the week and could see my frustration with the paint. When Allen was leaving he Hijacked the paint and some photo's, he knew I would use the paint on the engine later that week.

Well I must say that the following morning Allen had a local car repair shop mix a lovely colour, looked just like the photo's. At last I could apply paint and be sure the colour was good. The metal was lightly sanded with 400 grade wet and dry paper, degreased by wiping over with white spirit several times then finished off with a cellulose thinner wipe. Two good coats of Hi-build primer were sprayed on to the front wheels, belly tank and boiler lagging sheets. The following day these surfaces were lightly sanded and flattened with wet & dry sand paper. Later I applied three coats of two pack paint. This gives a very durable finish that is easy to clean and maintain, it will still be shining in ten years or more. Dave Prout's Burrell Shownmans engine Nancy was painted in two pack paint and still looks like new 14 years later. I name this paint, Allen Prout Green! In fact it has paint code of 1942.

 

Boiler lagging sheets & belly tank

Partially Lined front wheels

It is hard to determine colour with photo's, look at the difference of the front wheels and belly tank photo's. Obviously the camera flash is changing the image.

To apply the lining I have two types of tool. One is a professional BUEGLAR lining roller set. The other is a home made item that was made from an old draughting pen (placed on top of the roller set. Using these tools is easy BUT, it takes practice. You need to do a lot of practicing before you get the confidence to start applying lines to your single coloured parts. I usually find that the last parts you do have the best quality and you would like to start all over again!

Black painted Cylinder block, trunk guide support & wayshaft

The cylinder block assembly and trunk guide assembly was masked to allow me to spray it as an assembly. The inner surfaces of the trunk guides, valve spindles, Piston rod spindles and glands were all carefully taped up with tape. Stove enamel was applied in several thin coats by allowing the previous application to dry slightly first. This allow you to get a really thick of paint!

The Pre-painted lagging was re-fitted to the boiler, the boiler bands were attached loosely. Care was taken to measure their spacing to get them lined up and square. The brass bands were later used by the paint application roller as a guide to apply the lined bands. Note the paint that pulled off with the masking tape. Always a blasted curse!

Crank and flywheel during drying after painting, Coal Tub in the back ground!

Winch Drum Assembly

Painting the winch drum was an easy task. Just hoist it up, spray it black and let it dry!

Lots of work later!

The engine was run for it's firs steaming on May 5th. 5 hours of fun and anxiety were had, getting the engine out from the back yard, driving such a large and powerfully beast for the first time, taking care not to flatten the children that were all eager to get on for a ride. It is hard to put in to words what this is like. I found the Mc Laren was very able to produce steam. I feel that I had too much fire in the box, and with out the ash pan damper door fitted it would reach safety valve blowing off pressure in a very short space of time.

Boiler Steam Test details to be added later!

This article is under continual development. Call back later to see how the engine is progressing!

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